Region: North Sea, Norway
Well type: Newly completed producer
Challenge
A failed pressure test following the installation of a new completion in a North Sea oil producer led to the discovery of a 2 l/min. leak. The leak presented the operator with a diffi cult choice: undertake a lengthy troubleshooting process or
pull the completion. Further concern about wash-out damage to completion equipment made a quick solution imperative. Several leak sources were suspected. These included 3 gas lift valve (GLV) dummies and a chemical injection valve dummy. The completion also included a new packer, which had not been set, and a lower-set production packer. A plug at 3,827m limited the possibility of deeper leak points.
Solution
A LeakPoint survey was specifi ed and completed in under 10 hours. This precisely located a leak in the upper GLV dummy, which was retrieved and found to be damaged.
Case benefits
Key capabilities
Results
The LeakPoint survey provided the precise location of a diffi cult-to-pinpoint and potentially expensive leak. The survey also verifi ed the integrity of the other completion components within the well. The failed GLV dummy was replaced, a pressure test was performed and no further leakage was found. The customer stated that LeakPoint technology had helped to avoid lost production, re-completion and further intervention costs, saving the operator millions of dollars.
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